Practical Boat Owner – June 2019

(Sean Pound) #1
We were in Roscoff getting
ready to fill up with diesel fuel;
the tank was about quarter
full in our 36ft Najad. I cleared
the decks around the filler
and placed the funnel in the
neck of the filler. I was just
about to pour in some diesel
bug additive when to my
horror the little plastic sealing
cap from the diesel bug bottle
fluttered into the funnel and
down the fuel pipe!
I had disastrous visions of
this little plastic disc floating
around the tank then one day
blocking the feed pipe to the
engine at an inopportune
moment.
A kind bystander went to
the marina office to contact

the local engineer only to be
told that he was off for lunch
(at 1100) and was not sure
when or if he would be back!
So it was up to us to sort it
out. The flexible filler pipe
descends about 1.2m
vertically and was then jubilee
clipped to a right angled
stainless steel pipe welded to
the fuel tank. The obvious
thing was to disconnect the
two, having checked they
were joined above the level of
the fuel, but after an initial
attempt it became evident
that further manipulation was
very likely to break the
welded joint.
Plan B was to try and fish it
out from the top but a 1.2m

Vacuum to the rescue


Debris down the pipe! Simon James
saves the day with suction

4WD for the dinghy


came off, showing the piston,
stuck fast at the top of its travel,
with rusty, oily liquid as the
red-handed culprit.
I sprayed in some
penetrating oil and left it to do
its job, returning every evening
for a week to add more.
A sharp tap with a softwood
punch and a hammer moved
the piston a few millimetres.
Not wanting to force things, I
added more penetrating oil
and left it to do its work for
another 24 hours, before
returning. A few more days in
this vein and, eventually, with
the encouragement of a large
screwdriver used as a lever on
the flywheel, the piston moved
its full travel from top to bottom
and back again. The engine
was unseized!
On these engines the
cylinder is cooled with salt
water pumped around the
outside – simple, but it does
risk some corrosion – and the
large quantity of white salt
deposits and corrosion paid
testament to the fact that
maybe I hadn’t been as
fastidious as I should have
been about flushing through
with fresh water after each use.
Nonetheless, the metal
looked in a reasonable state,
so I poured in some white
vinegar. Next morning, the
deposits had all but vanished



  • dissolved by the vinegar
    acid. A scrape with a softwood
    lolly stick and a quick go with a
    vacuum cleaner left things
    looking much improved – the
    waterway was clear for the first
    time in a while!
    I poured in some more
    vinegar for the sake of clearing
    out any remaining deposits.
    Before reassembly I ordered
    a new cylinder head gasket
    from ebay for the princely sum
    of £8. A useful tip is that these
    engines were also badged as
    a Yamaha 2hp, so spares are
    interchangeable.
    Before refitting the cylinder
    head, I ensured both mating
    surfaces were scrupulously
    clean by using fine sandpaper
    on a flat surface and flatting
    back both engine block and
    cylinder head. This done, it
    was a quick job to reassemble.
    With a slug of fresh fuel in the
    tank, it roared (well, maybe
    groaned is more appropriate
    for such an old engine) into life.


Old age demanded
improved means of moving
the dinghy from the rack to
the slipway. First a pair of
wheels from an old
launching trolley were fitted
to the keel. I used a 10mm
threaded bar, but the

wheels had a 12mm bore.
Heatshrink tubing was
shrunk onto the bar in three
layers to provide a smooth
bearing. To lift the bow, I
modified an old golf trolley
that cost £3 from the local
recycling centre. Job done!

pipe was way beyond any
grabber that we had.
So onto plan C –
desperate measures. Out
came a 15mm dia plastic
pipe, a vacuum cleaner and
enough rags to seal the
plastic pipe to the vacuum
cleaner suction pipe. The
plastic pipe was inserted
into the filler pipe down to
the elbow and a couple of
minutes later I was able to
very carefully lift the disc out
to applause from the
growing audience.

James Brooking’s wheels idea


The disc inside the lid of
the fuel additive bottle
flicked straight into the
fuel funnel

The vacuum cleaner was
connected to a small bore
plastic pipe which was fed
down the fuel pipe

WARNING: do
not attempt
near petrol
fumes!

Fuel
tank

Welded stainless
steel elbow at the
back of the galley

Disc dropped as
far as this elbow

Fuel level

Filler

Jubilee clip

Jubilee
clip

Flexible
filler pipe
1.

2 m

Simon James’s Najad 360
Dolphy 8

C
F

ol
ey
Free download pdf