Motor Boat & Yachting — August 2017

(WallPaper) #1
The multi-chine hull needed
building up to give the new
Sleipner fi ns enough clearance

On the hard waiting for
the old Vosper mini fi ns
to be removed

All polished and
prepped ready for the
bow thruster propeller

The new bow thruster
tunnel gets glassed in
and built up in layers

Silver Echo is lowered
back in ready for her
fi rst sea trial

lorry with a tail lift and a pallet truck on board and
rented another two Transit vans towing trailers
(one of which diverted off to Poole to pick up our
new tender, an Avon mini RIB with a 50hp outboard,
sourced by the guys at boats.co.uk).
Despite being stopped four times by the police
to ask what was in the van, our trucks and trailers
made it safely down to Antibes. We spent a couple
of days afloat, prepping for the removal of the
KoopNautic system, and then it was off to Chantier
Bleumer at Baie des Anges where Philippe Hourez
once again helped us out with forklift trucks,
welders, polishers, antifouling and anodes, while
the guys from West Coast Marine got stuck into
the bow thruster and stabiliser job.
There were plenty of pumps to move around and
this time they were changing the position of the
fins from the very back of the engineroom to a
much more effective location at the front of it. We’d
noticed en route from Palma that being located so
far aft caused the boat to wander about, and even
the autopilot struggled to hold a steady course.


Sleipner agreed that the new position further
forward would be better, and thanks to the low
height of the SPS actuators (just 260mm), they
could be fitted under the engineroom’s floor plates.

HANDLING THE HYDRAULICS
Job one was ripping out the old bow thruster tunnel
and starting the long process of fibreglassing in the
new one, then grinding it down to leave a smooth
finish. The West Coast guys were working until 9pm
every evening to make sure that the next layer of
fibreglass would set overnight ready for progress
the following day.
This time we were tackling the hydraulic pipework
ourselves, both to save money but also to make sure
we got it all done while we were there. Everything
about the SPS 66 system is quite a bit heavier than
the fins we’d used on Silver Dee. The actuators are
105kg each, so getting those down the stairs and
into the engineroom was a mammoth task that
involved using a block and chain to lower them
into position. There was enough space in the

engineroom for the rack-mounted control system
but it was too big to go down in one piece so
everything had to be stripped off, and the rack
cut in half with a grinder before being welded back
together again in situ. For reasons of speed and
economy, we’d opted for one pump driven by the
starboard engine gearbox, even though Sleipner
recommends fitting two for redundancy.
Lots of other jobs were done during this time,
including ripping out four loos and replacing them
with Tecma toilets, changing the forward black
water tank for new fitted Tek-Tanks, plus many other
smaller jobs, so it was two weeks’ solid work before
we were back in the water and ready for the first sea
trial. The automatic bleed cycle seemed to work well
and the fins were moving across their full range on
the berth running off the auxiliary power pack. And
this time we’d even bought a hydraulic pump with
the right rotation!
We set to sea for the first sea trial and the fins
just locked over fully to port and wouldn’t move. We
could get them to centre up as we turned them off

SILVER DEE
James’s original
52ft trawler yacht

OWNER’S UPGRADE
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