A new bung fitting in the transom improved the boat’s seaworthiness
hull came away significantly at the
top – clearly the old bulkhead had
been partially responsible for
maintaining the hull shape. To
resolve this, we ran a lashing
around the boat to pull the sides
of the hull in to the bulkhead, then
used a dummy stick to transfer
the hull form to the plywood. A
few tweaks with the jigsaw and
a block plane gave us an
adequate fit to the hull.
We put the new bulkhead in
place with the hull held to shape
with a lashing. We then bonded
the plywood in to the hull using
wide glassfibre tape wetted out
with epoxy, and left it to set.
Once cured, we trimmed the top
to shape, cut a circular aperture to
fit a standard dinghy watertight
hatch and made a drainage hole
for a bung at the bottom. We then
made a centre support for the
foredeck using a length of studding
softwood and refitted a length of
the original hardwood to support it.
New gunwales
To replace the inner and outer
gunwales, we opted to use treated
softwood. Although not as durable
as hardwood, pressure-treated
softwood is cheap, lasts
reasonably well and, in this
case, is easily replaced.
We were able to buy the timber
in 4m lengths, saving the need to
scarf two pieces, but found that it
was not quite flexible enough to
bend around the forward part of
the hull. To solve this we built a
simple steam box using a metre
length of drainpipe, insulated with
an old curtain and with a wallpaper
stripper steamer inserted into the
bottom of the pipe.
Prior to steaming, we stepped
the forward ends of the inner
gunwales by 6mm to allow for
the foredeck. We then rigged our
steamer around an inner and outer
gunwale pair, aligned with the
Budget dinghy repairs
Conclusion
using clamps to hold the inner and
outer gunwales in alignment, we
screwed the two lengths together.
Once in place, we trimmed the
ends flush at the transom and
shaped them at the bow.
Replacing the deck
We took the easiest option to gain
the shape of the foredeck, placing
the sheet of 6mm plywood over
the top and drawing around the
gunwales. Allowing a 20mm
margin for the outer gunwale,
we cut it out and offered it up to
find it fitted adequately well.
To proof the timber against rot we
gave the new bulkhead, deck and
supports a coat of unthickened
epoxy before screwing the deck
into position and filling any gaps
with thickened epoxy.
Once complete, we gave the
whole lot a coat of Sandtex
textured masonry paint, left in
stock from a non-slip paints test.
O
ur aim was to get the dinghy afloat for minimum expense
of time and money, whilst doing so well enough that we
wouldn’t need to do it again every time we use the boat.
Everything worked well, with the exception of the Sandtex paint
which started coming off when scuffed around by feet and seawater,
leaving a milky residue. We were particularly pleased with how easily
the gunwales bent into place once we had steamed them.
We now have a useful, stable and seaworthy dinghy – apart
from the seven large holes we drilled for the transducers!
New foredeck spine in CLS softwood – we coated it with epoxy to prevent
it from rotting. Note the new gunwales, steaming in the curtain (top right)
Out on the water, testing forward
sonar units (PBO March 2016)
Clamping the
freshly-steamed
gunwales in place
before screwing
through to fix them
section of maximum bend.
As a rule of thumb, timber takes
about an hour per inch thickness
in the steam box to become
flexible. We withdrew the timber
after 40 minutes and found it bent
easily around the hull. Working as
quickly as possible down the hull,