A_T_I_2015_04_

(Nora) #1

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APRIL 2015
AEROSPACETESTINGINTERNATIONAL.COM

company proposed a number of design
changes to the blade to mitigate this
issue: the angle of the snubber face
was increased to 25° to make the
adjacent faces slide more easily and
an improved under-platform damper
was introduced to control the dynamic
response of the blade.

VALIDATION PROGRAM
Having identified the design solution,
the company’s efforts turned to
proving the change. It was established
that the design changes would be
validated by both rig testing and
engine running. The validation process
commenced with a frequency survey
of the revised blade standard and the
results compared with the data
previously available from the existing
standard. With the results of the
frequency survey in line with pre-test
FE predictions, the next step was a
fatigue test of the new blade. Six
sample blades were tested to establish
each of their failing fatigue strengths.
Each blade was mounted on a
vibration table and restrained at the
inner dovetail fixing and the snubber
to accurately represent engine
conditions. The rig used is shown
in the figure below right.
From the testing, it was
demonstrated that the basic strength
of the new blade was within the
scatter of the legacy blades and that
no new potential failure modes had
been introduced.

ENGINE TRIALS
Rolls-Royce followed a structured
process to establish the verification
and validation requirements for the
revised blade. It was determined by
the engineers that a number of engine
tests would be necessary to gather all
the evidence required to clear the new
blade for operational duty.
The last production engine was
shipped from the Rolls-Royce Filton
factory in 2005 and the testbed was
mothballed in 2010. Therefore
establishing an engine test capability
was the first major challenge. The first
of the engine tests, to calibrate the
testbed, was completed in May 2013.
With the testbed deemed serviceable,
the program to validate the design change
could begin in earnest. The first test of the
structured validation program was a build
of the engine, incorporating its existing
baseline configuration, against which the
intended design improvements could be
assessed. The build of the engine
incorporated two systems
to measure the dynamic response
of the blade.

between adjacent snubber faces is also
a major contributor to blade lock up.
In order to promote flutter during the
test, the fan assembly was built with
dry film lubricants removed and
snubber gaps at the bottom limit of
tolerance. Fan blade flutter can be
influenced by a number of factors,
the two principal being engine inlet
distortion and blockage downstream
of the fan. During the test program
the blockage in the front (cold) nozzles
of the engine was varied to further
promote flutter.
The first of these tests was completed
in September 2013 and featured the
existing blade fitted with the revised
damper. The purpose of the test was to
establish the individual benefit of the
damper, with the testing completed in
the flutter promoting configuration.
The next test, again in the flutter
promoting configuration, featured both
the revised blade and the damper. The
final test, completed in August 2014,
featured the revised blade and damper
in the production standard
configuration with all surface
lubrication reapplied. The results of
the test program clearly showed that
the redesign of the blade and the
incorporation of the new damper
led to a great reduction in flutter
amplitude of the blade. In the final
production standard configuration,
flutter has been all but eliminated.
Despite the twin technical and
logistical challenges, the Rolls-Royce
team compiled a comprehensive
understanding of the issue and devised
a substantial design improvement,
which is currently being evaluated by
the customer. z

Tim Williams is chief engineer – Pegasus,
transport and helicopter engines, with Rolls-
Royce plc, based in Filton, UK

900
The maximum range in nautical
miles of the USMC Harrier variant

1,347


The number of Pegasus
engines produced

9.25
The wingspan in meters
of the USMC Harrier

The first system is the blade tip
timing, which uses optical probes to
detect the arrival time of the tip of the
blade at a number of points around the
casing. The system measures the speed
of the engine spool and differences in
the time at which the tip of the blade
passes the probe compared with the
expected timing, and can be used to
determine the amplitude and
frequency of any blade resonance.
The second system is the FM grid,
and is similarly used to measure blade
dynamic response with a magnet
attached to the blade tip and a
conductive wire grid around the
engine casing. The motion of the
blade tip causes a signal to be induced
in the grid, which is proportional to
the frequency and displacement of the
blade tip and from which the blade
dynamic characteristics can be
deduced. Subsequent engine builds
and testing were aimed at
understanding the impact of the
individual improvements in the
proposed design changes.
As discussed earlier, the propensity
for flutter is dependent on the
lubrication of the snubber and other
contact faces on the blade. The gap

BELOW: (Below)
Vibration rig used
for blade fatigue
strength evaluation

z Harrier engine upgrade


ABOVE: Southern
Helmand province,
Afghanistan after
conducting an
aerial refuel
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