Plane & Pilot – September 2019

(Nandana) #1

16 SEPTEMBER 2019 ÇPlane&Pilot


PIPER PA28
Bonifay, FL/Injuries: 1 Fatal

The owner of the airplane experienced a partial loss
of engine power during takeoff following a touchand-
go landing, but was able to complete a 180° turn and
land safely back on the runway. During a post-landing
engine run-up, the owner was unable to duplicate the
problem, so he taxied to his hangar and reported the
problem to his mechanic. The mechanic, a commercial
pilot, subsequently boarded the airplane, performed
an engine run-up, which seemed normal, and elected
to fly the airplane around the airport traffic pattern.
A witness, who heard and saw the airplane on final
approach, stated that the engine was making “small
explosions” or “backfire”-like sounds. The airplane
subsequently collided with a tree before it impacted the
ground and a fence short of the 4000-foot-long runway
and was consumed by a postcrash fire.
Examination of the airplane revealed that the No. 4
cylinder exhaust valve was stuck in the “open” position
due to excessive deposits from the combustion process.
It is likely that the stuck exhaust valve resulted in the
partial loss of engine power. Maintenance records
revealed that the engine had not been inspected in
accordance with a manufacturer service bulletin regard-
ing stuck valves. Had the service bulletin been complied
with, it is possible that the accident may have been
prevented. Despite the partial loss of engine power
that occurred during the previous flight, the pilot flew a
traffic pattern that resulted in the airplane descending
into trees about 1/4 mile before the runway threshold
after the airplane experienced a partial loss of engine
power during the accident flight.
The pilot was diabetic, and although his blood glu-
cose was likely not very elevated at the time he died, it
was somewhat elevated on average over the preceding
few weeks. Elevated blood glucose can cause blurred
vision and subjective sensation of fatigue, as well as
increased thirst and urination. Unless life-threatening, it
does not directly impair decision-making or judgment;
thus it is unlikely that the pilot’s diabetes contributed
to the circumstances of this accident.

PROBABLE CAUSE(S): A partial loss of engine
power due to a stuck exhaust valve. Contributing to the
accident was the pilot’s decision to operate an airplane
with a known mechanical deficiency and his failure
to fly an appropriate traffic pattern that would have
allowed the airplane to reach the runway.

MOONEY M20E
Skyforest, California/Injuries: 1 Serious,
1 Minor, 2 Uninjured

The private pilot reported that, a few minutes after
departure for a cross-country flight and as the airplane
neared the top of a ridgeline, it encountered a down-
draft, aerodynamically stalled, and then impacted
terrain. One of the passengers reported hearing an
aural tone, which was consistent with the stall warning
horn, for several seconds before impact.
Weight and balance calculations determined that
the airplane was loaded near its maximum gross weight
and had exceeded the forward center of gravity limit,
which would have increased the airplane’s stall speed
during the accident flight. The calculated density
altitude was about 6,550 ft, which likely reduced the
available power and affected the climb rate.
A video of the final moments of the accident flight
showed the airplane about 25 ft above ground level
when the airplane entered a high pitch attitude, fol-
lowed immediately by a rapid descent, consistent
with an aerodynamic stall. According to the pilot,
the airplane was about 1,000 ft above terrain when it
stalled; however, given the location of the camera and
the pitch attitude that was observed, it is likely that
the airplane was within about 50 ft of terrain as the
airplane crested the ridgeline. The pilot should not have
attempted to cross the ridgeline at such a low altitude;
a higher altitude would have provided a clearance zone
to avoid turbulence and downdrafts. The pilot’s failure
to cross at a higher altitude resulted in the airplane’s
encounter with a downdraft with insufficient altitude
to recover from the stall.
The pilot reported that there was no evidence of
any preaccident mechanical malfunctions or failures
with the airplane that would have precluded nor-
mal operation.

PROBABLE CAUSE(S): The pilot’s failure to
establish the proper airspeed after departure and to
maintain adequate clearance from a ridgeline in high-
density and downdraft conditions and his subsequent
exceedance of the airplane’s critical angle of attack,
which resulted in an aerodynamic stall with insuf-
ficient altitude to recover. Contributing to the accident
was the pilot’s inadequate preflight weight and bal-
ance calculations, which failed to take into account
the gross weight, high-altitude conditions, and center
of gravity limit.

NOTE: The reports republished here are from the NTSB and are printed verbatim and in their complete form.
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