ELECTROSTATIC PRECIPITATION 289
at Column QQ36 at the +126−2 elevation. Detail B in
Figure 11 shows the ball bearing type that was selected. The
bearings (50 per assembly) were^7 / 8 in diameter, and were
made of M-50 steel as were the top and bottom assembly
plates. The ball bearing retainer was made of stainless steel.
The reaction of the G4 girder at Column QQ36 was 640 kips,
which ruled out a ball bearing design as the size that would be
required was too large for the space available. It was decided
to hang the huge girders in a pendulum fashion from a bracket
above, and allow them to expand by swinging. The connection
finally used is shown in Detail A in Figure 11. For the hanger
rod material, a high temperature service chrome-moly steel
was selected (ASTM 193-Grade B7). The bar material was
heat treated and stress relieved. Mill tests on the material used
indicated yield points of 98 KSI and higher. The total required
length of only 4¼ diameter rod was 19−10
Horizontal bracing has to be added to the 36 Column
Line to carry interior lateral loads out to the vertically
braced RR and MM column lines. This was accomplished
by adding two horizontal trusses, one at elevation 38-11
and the other at elevation 114−11 (see Section 2–2 in
Figure 11). It was possible to place the lower truss just
below the expansion connections for the precipitator sup-
port steel at elevation +42−8 so the “vertical” members
of the horizontal truss could also act as supports for the ball
bearing assemblies required for the lower units. This was
not the case for the upper units as the existence of other
steel (including the G4 girders) made it impossible to install
the upper truss any closer to the +126−2 elevation. New
support brackets were added to the 36 line columns to sup-
port the assemblies for the upper precipitator units.
The last major design obstacle to be overcome was the
exterior column movement that would result from the 2½
outward expansion of the framing at elevations +42−8 and
+126−2. It was accomplished by reinforcing the column
base billets (and in a few cases by extending the footings as
well) to transfer the eccentric column loads which would
be carried down predominantly by the exterior flanges.
Section 3–3 in Figure 11 indicates the type movement
expected. It was also necessary to cut free the support steel
of some platforms at elevation +25−2 so as not to restrain
the exterior columns close to their bases which would
induce high moment forces in the columns. This platform
steel was resupported on lubrite plate bearings before it was
cut free to expand. The column splice plates were found to
be flexible enough to carry the moments through the joints
at the expanding levels.
Construction Stage
Once the necessary alterations were designed and approved,
the difficult task of implementing the changes in the field
still remained to be done. One major limitation in this phase
of the job was that the precipitator erector was not anxious
to have any building connections cut free until his erection
work was essentially completed. He had placed a crawler
crane on a runway structure atop the 126−2 support steel
to erect the top units, and he felt that the vibrations already
being experienced with crane movements were large enough
with the original fixed connections in place, without increas-
ing them by adding expansion joints. This meant that the
expansion connections would have to be effected while they
were carrying their full design dead loadings. This loading
amounted to approximately half the total design load with
the remaining half consisting primarily of fly ash loadings.
The erection work was done in three separate stages.
First, the column base plates were reinforced as this material
was easy to obtain and required little fabrication. Second,
all the remaining work except for cutting free the expan-
sion connections was erected. That is, the bracing changes
required to fix the lower support columns, the stiffening
of the upper centerline support girders, the two horizontal
trusses along the 36 Column Line, and the brackets to support
the ball bearing assemblies. During this stage also, the ball
bearing assemblies were jacked up under the support gird-
ers, and the hanger rod connections at column QQ36 were
installed. The assemblies were positioned by jacking up the
support brackets. The G4 girder connections required the
hanger rods to be lowered down through the upper bracket
into position. After the top and bottom bearing and rocker
plates were in place, the upper nuts were then turned until
a snug fit was obtained. The third and final stage included
the actual burning free of the original bolted connections in
a very careful manner. Less than a sixteenth of an inch drop
was observed in the G4 girder elevation after the rods were
completely loaded at this point. The entire cutting operation
at all elevations was done in less than four weeks.
Operating Experience
All precipitator units have been operating successfully.
The tie-in to the boilers being done in two stages. The two
southerly units being connected first and then the northerly
ones directly after. This was accomplished by taking out the
south and north boilers alternately, thus reducing the rate of
the unit during this period to 500 MW. The complete tie-in
period was just less than six months.
Position readings of several exterior columns were taken
before any precipitator units were energized. Readings were
taken at the +42 and +126 elevations of each column mea-
sured. These “cold” readings were taken to obtain base mea-
surements from which to determine the outward movements
of the columns once in operation. “Hot” readings were taken
last summer with all the units energized and showed that
the north columns had moved a maximum of 1½ to the
north, and the east columns had moved a maximum of 1^11 / 16
to the east. Both north and east maximum movements were
recorded at the +126−2 elevation. Comparing this to the
design movement of 2½ it appears that the assumed steel
temperature rises were ample. The fact that the +126−2
framing is actually expanding more than the +42−8 fram-
ing is not surprising. It was expected that the upper reaches
of the building would be hotter by convection, and because
the elevation +126−2 framing has an operating unit both
above and below it. The lower elevation steel is more readily
cooled by outside air being pulled through louvers at grade
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