Figure 19 : Asset FMECA ExampleSEV = SeverityOCC = Occurrence Prepared by:Approved by:
DET = DetectionRPN = Risk Priority Number (SEV x OCC x DET) Rev. No.:Date:F# FF# C# FM# SEVOCCDETRPN SEVOCCDETRPN
1.0To be able to safely granulate and blend limestone, phosphoric acid and recycle at a rate of up to 350 ton per hour, while meeting all environmental, health and quality requirements (21% P and 15%
Ca)
1.3Unable to granulate and blend at all Main drive motor bearing seized Motor amps high lack of lubrication Vibration Monthly 8 3 3 72 0
1.3 Main drive motor bearing seized Motor amps high lack of lubrication PM route Daily 8 3 7168 0
1.31.3 Main drive motor bearingMain drive motor bearing seizedseized Motor amps highMotor amps high misalignmentmisalignment Precision MaintenanceVibration As NeededMonthly^8833351207200
1.3 Main drive motor winding failed Motor amps high insulation breakdown None 8 210160 0
1.31.3 Motor starterFluid drive leakingfailed Low oil level in reservoirPug mill alarm random reasonloose connections PM routeIR DailyMonthly^834334963600
1.3 Fluid drive crown tooth coupling seized Pug mill alarm lack of lubrication PM route Daily 8 1 3 24 0
1.31.3 GearboxGearbox seizedseized Pug mill alarmPug mill alarm lack of lubricationlack of lubrication Oil AnalysisPM route MonthlyDaily^8855262408000
1.31.3 GearboxGearbox bearing seizedseized Pug mill alarmPug mill alarm lack of lubricationlack of lubrication PM routeOperator Rounds DailyShift^8855321208000
1.3 Gearbox bearing seized Pug mill alarm lack of lubrication Oil Analysis Monthly 8 5 6240 0
1.31.3 Gearbox bearingGearbox leakingseized Pug mill alarmPug mill alarm lack of lubricationlack of lubrication PM routeOperator Rounds DailyShift^8355331204500
1.31.3 GearboxGearbox leakingleaking Pug mill alarmPug mill alarm lack of lubricationlack of lubrication Operator RoundsOil Analysis DailyMonthly^335544606000
1.31.3 Gearbox out put coupling (2)Pillow block bearings (2) seizedbroken spring Motor amps highPug mill alarm lack of lubricationlack of lubrication VibrationQPM MonthlyAnnual^4856331446000
1.3 Pillow block bearings (2) seized Motor amps high lack of lubrication PM route Daily 8 6 4192 0
1.31.3 Pillow block bearings (2)Cooper bearings (2) seizedseized Motor amps highMotor amps high lack of lubricationlubrication contamination PM routePM route DailyDaily^88666428819200
1.3 Cooper bearings (2) seized Motor amps high Improper installation Precision Maintenance As Needed 8 6 5240 0
1.31.3 Cooper bearingsCooper bearings seizedseized Pug mill alarmPug mill alarm misalignmentmisalignment Precision MaintenanceVibration As NeededMonthly^881135244000
1.31.3 Vessel shaft sealZero speed switch (2) failed openleaking Motor amps highPug mill seal leaking random stressesabrasive wear Operator RoundsOperator Rounds ShiftShift^289442726400
1.3 Zero speed switch wiring (2) failed to ground Motor amps high random stresses Operator Rounds Shift 8 4 2 64 0
1.3 Zero speed switch coupling (hose) (2) broken pug mill alarm random stresses Operator Rounds Shift 8 8 2128 0
1.31.3 Packing (2)Packing (2) wornworn No packing water flowPacking sleeve leaking excessively lack of water flowabrasive wear Operator RoundsOperator Rounds ShiftShift^2766252102400
1.31.3 Packing (2)shaft sleeve (2) wornworn Packing sleeve leaking excessivelyNo packing water flow abrasive wearlack of water flow PM routePM route DailyDaily^7261672521400
1.31.3 shaft (2)Pins brokenworn Wet product at discharge chutePug mill alarm overloadsabrasive wear Operator RoundsQPM ShiftQuarterly^26112848400
4.0Unable to meet quality requirements Paddles worn Wet product at discharge chute abrasive wear Operator Rounds Shift 6 2 8 96 0
4.0 Paddle shear bolt not relieving at correct shear point Wet product at discharge chute hard bolt Operator Rounds Shift 6 2 9108 0
4.0 Field start and stop station failed Machine does not start or stop random stresses None 8 110 80 0
3.0Unable to meet EHS requirements Machine guards damaged Defective guard wear or impact damage Operator Rounds Shift 5 2 1 10 0
3.03.0 Fume ductCentral lubrication system pluggedleaking No bearing lubricationHigh odor levels in room pinched lines or contaminationdefective joints or damaged piping PM routeOperator Rounds DailyShift^26212636800
3.03.0 Central lubrication systemLubrication pump inoperablebroken line Low grease line pressureLubrication pump fast cycling random stresseswear or damage PM routePM route DailyDaily^661533189000
3.03.0 Machine doorsLubrication system low air switch hard to removeinoperable at low pressure Door stuck closedHidden failure product build up around the door edgesrandom stresses 0 None 16 101101 6010 00
3.0 Pre-mixer discharge plugged Plugged feed chute high moisture content in the incoming material Operator Rounds Shift 8 6 2 96 0
3.0 Discharge chute plugged up Discharge chute plugged high discharge volume Operator Rounds Shift 8 10 2160 0
3.0 Base Crack/Corrosion Excessive vibration Vibration, Fatigue, Machine Load, Moisture, Damage to pug mill floor from cleaning Vibration Monthly 1 10 2 20 0
3.0 Vessel corroded Product leak moisture NDT Annual 4 1 2 8 0
POTENTIAL EFFECT(S) OF FAILURE POTENTIAL CAUSE(S) OF FAILURE CURRENT CONTROLS CURRENT PROCESS
FREQUENCYKNOWNFUNCTION FUNCTIONAL FAILURE COMPONENT POTENTIAL FAILURE MODE(S)FAILURE MODE, EFFECTS, AND CRITICALITY ANALYSIS (SFMECA)
ACME AggregatesGranulation
J. Doe Smiley^1System:Plant: Tim Richter
Subsystem:Analysts:
ASSESSMENT (AS RISK
IS)
ASSESSMENT (TO RISK
BE)TASK FREQUENCYRESPONSIBILITY /DATE9/23/2013
RECOMMENDED RISK MITIGATION ACTIONS