Fly Past

(Rick Simeone) #1

90 FLYPAST November 2018


FROM THE WORKSHOP ENGINE RESTORATION


with the propeller and pitch control.
It would have been wrong not to
try to achieve this, as the parts had
essentially stayed together for
41 years.
Although the engine would be
for ground-running alone, I
wanted to restore all parts to
the appropriate standards and
condition, as specified in the
manufacturer manuals.
It was obvious from the outset I
would need to source a significant
number of type- and age-related
components for a fully functioning
engine. This aspect was exciting
and no different from whether you
are restoring a 1926 Royal Enfield
motorcycle or an Avro Anson C.19
engine. It’s a case of continuous
searching and, sometimes,
outstanding luck. Even as-new
items in the original packaging
would be sourced.
In May 2012, I was fortunate to see
the remains of Anson C.19 TX226.
If the undercarriage assembly
could be obtained, could it be
incorporated as a fully functional
system? The exhibit could then
be representative of a complete
engine/undercarriage assembly.
And the paths of TX226 and
G-AGPG were on a metaphorical
collision course.
Approval to purchase the
undercarriage was given and the
assembly was removed in October



  1. The scope of the project was
    complete: a fully functioning Anson
    engine and undercarriage, with
    instrumentation and controls from
    two known aircraft.
    I may be corrected by Avro
    engineers, but I do not believe it
    was ever intended to be able to
    remove the C.19 undercarriage as
    a complete unit. With two friends, I


dismantled the assembly over two
days, but it was far from easy.

Oxidisation battle
Rrestoration of the engine began in
February 2012 and was completed
by October 2013. It was stripped
into its individual components and
each item examined for wear and
damage, dimensionally checked and
overhauled. There was considerable
corrosion on two of the cylinder
bores and associated valve gear.
However, considering the engine
had been stored outside, it was,
internally, in surprisingly good
condition. Because of this the
crankcase, reduction gear box and
auxiliary drive gearbox were not
disturbed; just two replacement
cylinders had to be sourced. But
piston rings, four per piston, were
a different issue. Most of the rings
where badly carbonised and could
not be removed, so replacement
rings had to be sourced. This was
a surprise as the aircraft logs
indicated the engine had only run
for 138 hours of the 600 available
since the engine was reinstalled
following its last service.
Design and development
of the support structure and
trailer continued in parallel. The
complexity of the trailer had been
increased significantly to meet the
aim of running the full propeller
(regarding thrust loading and
ground clearance) and to allow the
undercarriage to raise and lower
fully. The mounting height of the
complete assembly was critical,
not just to meet ground clearance
issues, but also to ensure the trailer
was stable during towing.
The undercarriage mechanism can
only be described as a wonderful
piece of mechanical engineering.

However, in common with the
difficulty of removing it from the
airframe, it was also troublesome
to dismantle and restore to working
condition. Sourcing the missing
parts for the undercarriage, wheel
and axle, was also challenging, but
it was a case of ‘keep looking’ and,
just like buses, two often came
along together.

Good progress
In common with all other aspects
of the project, the aim for the
controls and instrumentation was
to be as authentic as possible.
For the engine, propeller and
undercarriage controls, this was a
straightforward case of restoring
the original G-AGPG equipment.
The instrumentation meets all
the engine and auxiliary services
requirements and is consistent with
type, and fully operational.
The final item for restoration was
the Rotol propeller, and this was
the most challenging but rewarding
part. This prop is the original Rotol
constant speed variable pitch type
R30/242/1 unit fitted to G-AGPG in
June 1958. It was last serviced in
January 1968 and, by the time its
use was discontinued in 1971, just
110 hours of its 1,000-hour life had
been used.
Having spent the last 41 years
outside and moved around the
country, it was in surprisingly
good condition. The chips and
dents on the trailing edges were
all repairable and the hub had only
superficial surface corrosion, but
there was deep corrosion on the
external surfaces of the balance
weight-retaining ring, pre-load and
retaining nut. However, they were
all recoverable and, thankfully,
when completely dismantled

propeller internals were also in
excellent condition.
Without a complete copy of Air
Publication 1538E Rotol External
Cylinder Variable-Pitch Propellers


  • Instructions for Repair and
    Reconditioning, this task was a non-
    starter. The tooling requirements
    for the propeller restoration were
    significant, not just for dismantling
    and assembling, but for the
    balancing and setting of the pitch
    angles. All the tools had to be made.


Trial run
On June 12, 2018 the assembly
was rolled out from the workshop
and the propeller fitted along with
the spinner. The restoration was
effectively completed and ready
for towing tests and engine-
running trials.
After a few failed attempts
at starting, the procedure was
changed, and the engine then
jumped into life first time. It runs
very well, starts reliably and the
prime engine parameters, oil
pressure and temperature are
within specification.
The annual Avro Heritage Trust
Air Fair was held at Woodford On
July 7-8, 2018. On the Sunday,
Peter Kosogorin flew the BAE
Systems Heritage Flight Anson,
G-AHKX, providing a beautiful
spectacle. His excellent display
took him directly over the
restored engine of G-AGPG and
the operational undercarriage of
TX226, which performed faultlessly
at its first public display. As a
bonus, inside the Avro Heritage
Museum was the resident cockpit
of G-AGPG, restored to its EKCO
Avionics format. Anson overload?
Probably. But you can never have
too much of a good thing.

Engine restoration complete: the purpose-built
maintenance stand was employed throughout
the rebuild and allowed the engine to be
rotated through 360 degrees.


The undercarriage unit fully dismantled, ready for restoration. Cleaning, inspection and cosmetic
restoration were required before its rebuild.

This rear view shows the original wing rear
spar anchor point for the engine bearer struts,
as well as the mainwheel fork link and the
pilot’s control suite.
Free download pdf